Clutch Damage: Torque Tube Moved Forward

Drive Train

Clutch Damage: Torque Tube Moved Forward

I removed the clutch cover from my 86.5 for release bearing replacement, and found that the
forward end of the stub shaft (the large clamp) has been rubbing severely against two bolts that
attach a plate across a frame (very technical) to the point where the bolt heads are virtually
gone, and I do mean GONE. Finding the means to remove and replace them is going to prove
difficult! I also suspect that the groaning/squealing I have been hearing is probably related to
this problem, and not the bearing.

My question: What would cause the shaft to move forward this much? Is this movement some
function of normal clutch wear, and in my case, excessive wear, or something entirely different?


I have a bad feeling about this, so all replies appreciated!

Suffering performance withdrawal symptoms....

Marty
86.5 Indischrot 5-speed


If your pilot bearing is shot and either or both couplers that clamp the torque tube to the central
shaft or the transaxle are loose, then the central shaft and possibly the torque tube may have
crept forward.

--Patrick
79 hybrid
84 stock


Yes, indeed, it now appears that the torque tube shaft is the culprit.

Has anyone else experienced this "creeping" shaft that moves forward within the torgue tube
housing?

I'm moments away (well, some moments anyway) from starting the awful removal process, and
would be delighted if someone came forward with a 5-minute fix that I somehow missed (hope
springs eternal).

Barring that, any helpful hints on pain-free TT removal will be welcomed!

86.5 Indischrot 5-speed
Very blue owner :¬(


If you have been following my posts, I have been experiencing a clutch/torque tube problem
that is almost answered, though not resolved.

Thanks to advice from Mark Anderson, I checked the rear coupler on the torque tube, and it
appears that the coupler was loose allowing the shaft to "work" and wear down the splines. As
it did so, the shaft inched forward to the point where I see what I think is the bolt groove
emerging from the female end of the coupler.

My question (there really is one) is this "Is there more than one groove on the gearbox end of
the shaft? I suspect the answer is no as I can also see what appears to be remains of splines!


I have attempted to remove the bolt to verify if the "groove" is where it is supposed to be, but
the bolt is "weld-tight" which I would expect if it were worn and in an interference fit. This little
jewel of a problem will
be interesting to overcome!

It was mentioned that a problem like this is rare, so I guess I have a "rare" shark!


So, here's a summary of the problem.

The rear coupler bolt apparently loosened, and allowed the driveshaft to "work" inside the
splines. Over time it eroded the splines and somehow caused the shaft to inch forward. This is
hard to figure as the press fit of the shaft into the bearings would (I thought) have prevented
any fore/aft movement.

As it inched forward, the bolt wore a flat spot (sort of) back along the splines. This flat spot
was the only thing preventing the shaft from rotating completely in the rear coupling. Once the
bolt was removed, the
shaft could be spun quite readily!

To get the bad shaft out, I had to pull the transaxle and torque tube without being able to slide
the front coupling off the stub shaft. This was not easy as clearance is a big problem.

With the torque tube/transaxleout, I next had to cut through the torque tube just in front of the
transaxle and slice the driveshaft. This allowed me to reomove the torque tube proper. and then
get to the frozen rear bolt. Getting the rear bolt and shaft remains out proved easy. Amazingly,
the input shaft to the gearbox was undamaged!

At the front of the assembly, I had to replace the pilot bearing as the creeeping driveshaft had
punched the guts out of it! Removing the remains of the bearing was a real bear. Also affected
was the throwout bearing sleeve and the bellhousing where the vibrations up front (from the
failed pilot bearing) loosened the sleeve and allowed it to "fret" the bellhousing surface.

All in all, my parts costs were low, but my "internal" labor costs were exceptional! I estimate I
have spent 30+ hours getting this problem fixed. This includes all the "special" tools I have had
to fabricate to remove items in a non-standard fashion.

I strongly encourage owners who have had a torque tube removal to have the coupler bolts
checked for torque at some rather short interval, say 500 miles. To have this extensive a repair
done at a shop would have been devastatingly expensive!

Warm regards,
Marty
86.5 Indischrot 5-speed

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